Cracks, Bolts, Nuts...

Fixing Cracks Under the Starboard Side Genoa Track

Spring 2001

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NOTE : Please do not follow the advice below with regards to the cabin woodwork; I have since been reliably informed that it is possible to remove the starboard side cabinetry without disassembling it, so access to the nuts underneath the genoa track should not be a problem. I will post details of the procedure if I ever manage to track them down...

This documents a project to remove the starboard side genoa track to fix water ingress through the track bolt holes, check the extent of damage to the core, and investigate associated hairline cracks.

It is probably worth noting that I am extremely reluctant to drill holes anywhere in the boat - this is my minimalist solution. A neater but far more challenging approach would entail disassembling the entire starboard-side cabinetry - it's your choice...

Lexicographical note - for those under the linguistic influence of the United States, a spanner is the proper word for a "wrench".

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In_place_1_th.jpg (2803 bytes) The original problem. These hairline cracks appear to be letting water seep into the deck (and core - yuk!); found water accumulating in a cabin light fitting immediately underneath one of the bolts.
_015_th.jpg (2846 bytes)
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Internal_access_1_th.jpg (2967 bytes) This is going to be a pain - there is almost no access to the nuts on the genoa track bolts without disassembly of the starboard side cabinets - major work. I am considering cutting out access holes that will be covered by the trim (removed, not shown).
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_001_th.jpg (2826 bytes) _002_th.jpg (3427 bytes) _002_th.jpg (3357 bytes)
So here's the method used : drill large holes either side of each bolt, and chisel out a section. This gives enough access to hold the nut while a hardy soul on deck unscrews the bolt. As the track and through-deck holes are not threaded, you will also need to apply pressure underneath the bolt to get the screw-head to rise out of the track. Then extreme dexterity is required to gather the nut, lock-washer and load washer before they roll gaily off into the inaccessible nether regions of the cabinets.

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_003_th.jpg (2826 bytes) This is the toughest bolt - right above the galley/main cabin bulkhead, with a fibreglass liner immediately below it. Requires drilling, chiselling and hammering to clear access to it. In the end, I also attacked the liner section over the stove with a Dremel tool - not as ugly as it looks here, and largely irrelevant cosmetically as all this damage is covered by the decorative teak strip that covers the access holes.

This also shows the galley section that has pre-cut access holes - very thoughtful, but what about access to the 15 nuts forward of this?
_006_th.jpg (3338 bytes)
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_005_th.jpg (3080 bytes) Tool tips - on the left, the set used for getting access to the bolts; the chisels also function as rasps to smooth off the corners. The pliers are helpful in pulling the wood chips out rather than letting them fall back. Of course, we need a work cloth and vacuum cleaner to keep everything tidy...

The tools on the right illustrate a couple of useful tricks in getting the nuts and washers off; once a nut is almost off, cover the bottom of an open-ended spanner to capture the nut while the bolt is unscrewed; the sharp pick (a generally useful tool) helps to retrieve the washers.
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_010_th.jpg (4371 bytes) View from the outside - the track has been removed, leaving 20 years of grime and 30 holes. We used the adjustable spanner on the square-shafted screwdriver to shift the tighter bolts.

After cleaning, a close-up of the bolt holes seems to confirm that the deck cracks are not structural. The good news : it appears that this area of the deck (about 5/8 in. thick here) is cored with ply rather than balsa, and all core is at least intact and generally in decent condition - no significant water damage here.

Note the countersinking on the holes - supports packing with sealant.
_012_th.jpg (2470 bytes)
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_009_th.jpg (3150 bytes) The one that didn't get away - this bolt would not budge out of the track (shown removed and inverted), even with two broken screwdriver bits and an impact driver. As this was the only stubborn bugger, and we were able to remove the nut below, we levered the rest of the track up and left the solitary bolt to soak in penetrating oil, contemplating its fate. After an hour or so, we wellied (technical term) the bolt with a hammer (note protecting nut), and convinced it to give itself up.

There was significant corrosion around several bolt holes; not sure of the reason (why one hole and not another?), but I will apply aluminium/steel anti-corrosion gel around the upper section of each bolt when refitting.
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Refitting came after cleaning everything up - the deck holes, the track and the bolts - using a variety of power tools, hand tools and elbow grease.

After much consideration, we came up with a cunning plan (so we believe) for refitting the track bolts with a maximum of sealant in the right place, rather than pushed through the hole on the tip of a bolt. Raising the track an inch or so off the deck with old pieces of hose, we dry-fitted the bolts through the track and into the deck; then we applied sealant to the circumference at deck level of each bolt as it was slowly turned. This seemed to drive the sealant into the counter-sunk deck holes quite nicely, and when we pressed the track and bolts down, there was just enough squeezed out to indicate a good fill.

In the end, I decided against putting anything around the heads of the screws or the track holes for two reasons : Back on the inside...

When replacing the nuts on the bolts, I found that more room was needed, and eventually had to cut out most of the length of the board, to get two fingers on each nut while holding up the load and lock washers - compounded by the distortion of the bolt tips caused by them being trimmed with bolt cutters when originally fitted... The original small (0.5 in.) load washers were replaced with larger ones (up to 1.5 in.) on refitting, to distribute the load over a wider area.

Definitely a two-man job. Special thanks are due to Jim for providing the extra pair of hands, a resourceful brain, and the odd tool; his advice, help and patience were much appreciated.
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